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Loop 286 at Spur 139 Crossover Removal Narrative <br />The proposed safety enhancement at this location consists of removing the existing crossover.. <br />This corridor has an ADT of 27,202 vehicles per day. The estimated cost for this work is <br />$29Q,327.40. The Safety Improvement Index (cost benefit ratio) of this project is 13.63. <br />Some potential benefits of this enhancement include: improving traffic safety, increasing through <br />capacity and reducing delays. From 2017 through 2019, 3 accidents have occurred resulting in <br />3 non -incapacitating injuries due to utilization of this crossover. Other accidents such rear end <br />collisions caused by vehicles slowing down to utilize the crossover and other related accidents <br />are not included in the previously noted data. Because of this, it is reasonable to assume that <br />many additional accidents could have likely been prevented had the crossover been removed. <br />Removal of the crossover would require vehicles to utilize the following crossovers to cross <br />Loop 286. Northeast bound traffic would utilize the Stillhouse Road underpass as a crossover, <br />which would result in an increased round trip travel distance of 2.88 miles. Southwest bound <br />traffic would utilize the FM 195 underpass as a crossover, which would result in an increased <br />round trip travel distance of 1.66 miles. <br />Loop 286 at Clement Road Crossover Removal Narrative <br />The proposed safety enhancement at this location consists of removing the existing crossover. <br />This corridor has an ADT of 27,202 vehicles per day. The estimated cost for this work is <br />$290,750.90. The Safety Improvement Index (cost benefit ratio) of this project is 22.68. <br />Some potential benefits of this enhancement include: improving traffic safety, increasing through <br />capacity and reducing delays. From 2017 through 2019, 5 accidents have occurred resulting in <br />5 non -incapacitating injuries due to utilization of this crossover. Other accidents such rear end <br />collisions caused by vehicles slowing down to utilize the crossover and other related accidents <br />are not included in the previously noted data. Because of this, it is reasonable to assume that <br />many additional accidents could have likely been prevented had the crossover been removed. <br />Removal of the crossover would require vehicles to utilize the following crossovers to cross <br />Loop 286. Northeast bound traffic would utilize the Stillhouse Road underpass as a crossover, <br />which would result in an increased round trip travel distance of 2.28 miles. Southwest bound <br />traffic would utilize the FM 195 underpass as a crossover, which would result in an increased <br />round trip travel distance of 2.28 miles. <br />